GaryDoug
First Officer
Flight distance : 1264639 ft
United States
Offline
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I had two motor failures on my backup Mini, both fronts. More detail on that in another topic.
But after ordering two arms with motors, I wanted to disassemble a motor after it was removed from the arm, so I fabricated a very cheap tool to do the job. I cut a 1-1/2" long piece of galvanized steel electrical conduit pipe, which was the perfect size for the motor. It was necessary to cut a slot in one side to accomodate the cable. I do not have a shop press but I was able to easily use an ordinary small drill press. For a press tool, I used an ordinary 1.5" finishing nail with the head and point cut off. It was the prefect size to press out the center pin. Place the motor onto the pipe with the housing end up and push out the armature and axle pin by pressing down about 1/2". If you are using a drill press, do NOT have it running. To reassemble the motor it was much simpler, just push the armature into the housing and press it down with just about any available blunt tool.
Pressing out the pin/armature will deform the housing slightly, but that will return to normal when you press the armature back into the housing.
I was able to clean out the loose iron particles and reassemble the motor. It ran fine for 10 minutes, but I do not trust it to not release more particles, so I installed both new front motors/arms.
What I found inside was a lot of very small pieces of the laminated cores that were jamming the motor, no sand. But that's another topic for now.
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