DawgPound2
lvl.1
Flight distance : 24938 ft
United States
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HELP! Ok, so I was preparing to fly my bird the other day on a construction job site when I was having issues getting clearance to fly in a Class D airspace, but that's another issue. I picked up my Phantom 4 and went inside the job trailer. In order to hold on to it, the controller, and open the door, I held it upside down by the landing bar/gear.. whatever you call it. I've done this before and haven't had an issue. But I want to give as much detail as possible here. Anyways, when I set the drone on the table, what appears to be the pitch motor, began to squeal and it struggled to move, going about it in a spastic manner. I shut it down and started it back up and it again made a squeal about the pitch motor. Then it just pointed down and was completely unresponsive. I have gone through an IMU calibration along with a gimbal calibration. Neither made a difference. So, did I kill the motor by turning it upside down? Could it be a belt? Also, the firmware seems to be up to date. The DJI Go 4 app isn't telling me otherwise. Any ideas?
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