TN Lone Wolf
lvl.3
Flight distance : 963251 ft
United States
Offline
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Hello all, it's been a while since I've been on here.
I'm attempting to debug a Phantom 4 Multispectral problem. When my coworker and I tried to map with it, we discovered that the camera refused to maintain nadir and would arbitrarily pitch from 90° downward to 0° level at the conclusion of each leg of its mission, and it would stay 0° level without our input. As a result, even when we tried to manually aim the camera back down using the controller's camera pitch wheel, we couldn't complete a mapping operation. While attempting to troubleshoot the issue in free flight mode in Ground Station Pro, we noticed that the camera would begin to pitch up and down when the drone came to a stop.
All equipment, software, and firmware are fully up-to-date, and the aircraft has been calibrated. This is the first task we attempted with it out of the box. We used Ground Station Pro and Photomap mode using default settings to perform the flight.
Any help would be greatly appreciated!
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