Cory W
lvl.3
Flight distance : 137953 ft
Canada
Offline
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Hey everyone,
I've put my M600 together with no problems, finally got everything done and ready for 1st test flight. My self and my buddy went out in a safe location for my first test flight, software up to date, did compress calibration, batteries fully charged, remote controllers as well, not any type of signal interference, we were in a forrest area, middle of no where. M600 was in PGPS mode with 19 sats, DJI go app said on top left corner IMU initializing then said safe to fly. fingers crossed, started motors, did my little pretest of making sure motors were respawning to remote controller, things seemed good, gave about 40 percent to left air craft to about 6 feet, then I never gave any movement of sticks, 2 seconds later the drone start dafting by it self, moving soft of in a forward circle pattern, I started to try to get air craft under control again, I stayed calm the whole time this was happening, after about 43 secs of its doing this, I got it to a slow down enough speed to land it, flying my inspire 1 for about a year really helped me in this event, if I had no drone flying experience, it probably would have crashed
After all that happened, me and my buddy thought maybe compress calibration did not work the first time, so we did another one, in my calm mode, I started it all over again and same thing happened again but this time is was like for 1:17 secs, safely landed it again. I went over my DJI go app flight log and speed was around 1.5 M/S sometimes, I think I did well in preventing a crash twice. We have thought about everything that may be causing this prblem again, then we realized we have failed to do a IMU calibration when I put air craft together
does anyone think that is probably the problem ??
Thanks
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